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thummmper Samba Member
Joined: November 25, 2009 Posts: 2015 Location: Meadow Valley, California Republic
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Posted: Sun Jan 20, 2013 8:04 pm Post subject: |
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arrow marks park position
comparison
ready to go back in
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Vanagon Nut Samba Member
Joined: February 08, 2008 Posts: 10371 Location: Sunshine Coast B.C.
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Posted: Sun Jan 20, 2013 9:16 pm Post subject: |
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Who knew?
Chrysler part?
Neil.
[quote="thummmper"]
comparison
_________________ 1981 Westy DIY 15º ABA
1988 West DIY 50º ABA
VE7TBN |
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tristessa Samba Member
Joined: April 07, 2004 Posts: 3992 Location: Portland, OR
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Posted: Sun Jan 20, 2013 10:15 pm Post subject: |
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What, the VW arm didn't fit the Chrysler wiper motor? |
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D Clymer Samba Member
Joined: December 22, 2005 Posts: 2978 Location: Issaquah, WA
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Posted: Sun Jan 20, 2013 10:30 pm Post subject: |
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Interesting, Todd! It seems that many oem components in the automotive industry share very common configurations. I already noticed this with your Chrysler steering column retrofit and just how similar the Chrysler part was to the VW part. Now this wiper motor with common bolt pattern and shaft design just further proves the point.
Keep up the good work!
D |
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MidwestDrifter Samba Member
Joined: June 13, 2012 Posts: 769 Location: Kicking Around Australia
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thummmper Samba Member
Joined: November 25, 2009 Posts: 2015 Location: Meadow Valley, California Republic
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Posted: Tue Jan 29, 2013 8:33 pm Post subject: |
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onward
got lucky with the clearance
the hardest part was getting the washer hose back on the spray tip- it all had to come back out for that.
and this is the 13 dollar wire bundle I got from a 95 caravan
the powerbox is split and flipped for the connections forward- the on-off and intermittent relays
so now the dash is back in and the splicing continues
I got on the clock [10 days] for my AR from jd machine! trigger lower.
I also got a new drivers lic and thank the lord it doesnt have a chip on it. |
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thummmper Samba Member
Joined: November 25, 2009 Posts: 2015 Location: Meadow Valley, California Republic
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Posted: Sat Mar 02, 2013 5:31 pm Post subject: |
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cruise control servo is in
and the ac is coming along
I redirected the stub out tubing, but I don't know if they are crimpable
cc servo bracket is removeable
pump bracket just before install
I have my lengths and the dryer is on the way from bus depot [42.00]
the one low return from the condenser hose is made [77.00] and I want to have a single made from the cooler overhead to the high side of the pump. then there is the condenser to the vacuum/low side of the pump [it's almost 8 feet longer] |
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thummmper Samba Member
Joined: November 25, 2009 Posts: 2015 Location: Meadow Valley, California Republic
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Posted: Sat Mar 16, 2013 11:52 pm Post subject: |
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hoses for two vans
the hi-low switch hose is the most tedious to rehose
and the theft of collars from new fittings
got me 6 of eight hoses needed for 2 vans for 290 bucks
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thummmper Samba Member
Joined: November 25, 2009 Posts: 2015 Location: Meadow Valley, California Republic
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Posted: Tue Mar 26, 2013 10:49 pm Post subject: |
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I finally finessed the pump connections--now I am waiting for 2 idler bearings from texas at 37.00 each compared to the serpentine tensioner bearing at 8.00 ea. maybe I can do a mod for the latter in the former. but I'm moving forward now.
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thummmper Samba Member
Joined: November 25, 2009 Posts: 2015 Location: Meadow Valley, California Republic
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Posted: Wed Mar 27, 2013 11:04 pm Post subject: ac stuff |
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vacuum lines for the cruise servo
and the v belt is tight too with a new idler bearing
put the wipers back on and the courtesy lamps are coming along--I want to convert the headlights to my 92 Toyota pickup--they are the exact same shape and dimensions, but they are sealed halogen beams with no o-rings to fail. just when I get close to being driveable, I decide to solve something else..but she needs back on the road as the trep just boiled over slightly and her engine needs the reseal treatment. so balance calls it--next week I'll be on the road again |
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thummmper Samba Member
Joined: November 25, 2009 Posts: 2015 Location: Meadow Valley, California Republic
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Posted: Wed Apr 03, 2013 3:39 pm Post subject: |
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interior lights are electronically controlled now using vanagon wires mostly and Chrysler module and lights
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shadetreetim Samba Member
Joined: January 10, 2011 Posts: 1994 Location: Riverside, California
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Posted: Wed Apr 03, 2013 6:12 pm Post subject: |
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Illuminating post _________________ Tim Potts
Doing my best every time I drive it to dispel the myth these Vanagons have to be slow!
'89 Vanagon Bluestar/Country Homes 1.8T & .77 4th
'74 Jeep CJ5 |
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r39o Samba Polizei
Joined: May 18, 2005 Posts: 9800 Location: San Diego
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Posted: Wed Apr 03, 2013 7:12 pm Post subject: |
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Can ya roll it down PCH on Sunday?
FYI. Your phone seems to just ring....... _________________ "Use the SEARCH, Luke" But first visit the Vanagon FAQ!
1990 Multivan EJ 22, Rancho trans 0.82 4th, Small Car front AC, CLKs w/ 215/65-16, homemade big brakes 303mm, Konis, Recaros, etc....
Click to see my ads for Cup holders, Subaru clutch fix and CLK wheels (no wheels currently) |
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thummmper Samba Member
Joined: November 25, 2009 Posts: 2015 Location: Meadow Valley, California Republic
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Posted: Tue Apr 30, 2013 9:45 pm Post subject: |
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just liberated said van from mcpeek dodge in Anaheim and after a diagnostic for dying with any gas pedal, it was found that I cut a 5 volt feed wire from the brain within a 3 wire tail that fed an unemployed low speed Chrysler radiator fan plug that was sticking out of the bundle just north of the ac pump. in my "why not" paring excersize, I effed myself. Without the feed there, which was spidered in and should have just been taped up, the throttle position and manifold absolute pressure sensors were starved of voltage and the engine would not move from start mode to run mode.
another lesson for the archive. I believe it was a violet/white wire. pcm pin number 6. I have been so stressed out thinking this could kill the project that I tortured myself with dread. only after I fealt her on the road heading south did I realize just how miserable I no longer was.
I am after the fuel tank remedy next, with bedseat mixed in.
in a month I will take her back for a transaxle diagnostic to find out why the converter doesn't lockup until 84 mph. 42 is normal. its not a young trans. but it will make me proud at the pump again.
Last edited by thummmper on Tue Jul 09, 2013 7:30 pm; edited 1 time in total |
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luVWagn Samba Member
Joined: February 21, 2008 Posts: 1340 Location: Snoqualmie (WA)
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Posted: Wed May 01, 2013 1:34 am Post subject: |
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thummmper wrote: |
only after I fealt her on the road heading south did I realize just how miserable I no longer was. |
I love your build, and your quotes. Happy to follow along as an innocent observer... _________________ '91 Syncro 16 Reimo Hightop Conversion, eTDI |
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thummmper Samba Member
Joined: November 25, 2009 Posts: 2015 Location: Meadow Valley, California Republic
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Posted: Sun Jun 02, 2013 8:24 pm Post subject: |
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the OE tank mods are complete-- for state inspection, the last issue-
I should have done this at the start
all that and it only had six leaks, which the white eastwood sealer cured.
Last edited by thummmper on Tue Jul 09, 2013 7:33 pm; edited 1 time in total |
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Phishman068 Samba Member
Joined: February 19, 2007 Posts: 1867 Location: Pittsburgh PA (ish)
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thummmper Samba Member
Joined: November 25, 2009 Posts: 2015 Location: Meadow Valley, California Republic
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Posted: Mon Jun 03, 2013 6:51 pm Post subject: |
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it does have a lower deck to clear the coolant tubing and the shifter on the left. It probably is, but I need a stock looking bottom with not only a modern pump module, but the shape to fit around the upgrades. |
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thummmper Samba Member
Joined: November 25, 2009 Posts: 2015 Location: Meadow Valley, California Republic
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Posted: Thu Aug 29, 2013 12:52 am Post subject: |
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I still haven't been back to the ref as I spun a rod bearing on july third--#5 cylinder. I thought it was a lifter at first and drove it 6 miles home as it really started banging and I shut it off. the piston was hitting the head, as seen here on the center piston [light spots], but not enough to damage it. the heads got rebuilt and a light surfacing with new seals
and before this happened, I drove her back to the driveway I first found her in, in Belmont shore, California, that june 12, 2010
and just 3 scant years later with almost everything reengineered
I also worked out a mod for the headlight adjusters with a cv type floating nut design and a surfaced pair of 8mm nuts that socket the adj screws--all steel parts
Last edited by thummmper on Wed Oct 23, 2013 1:35 pm; edited 1 time in total |
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thummmper Samba Member
Joined: November 25, 2009 Posts: 2015 Location: Meadow Valley, California Republic
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Posted: Wed Oct 23, 2013 12:59 pm Post subject: |
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So, I tore her down to the short block and sent her out to the engine builder-in early august. -10-10 crank on the rod journals and a polish on the mains--reusing the 5 pistons and rods and replacing the 0ne piston and rod-[I would have reused the piston]
new bearings and freeze plugs, block clean and lump returned, no oil pump or heads, $1700.00.
the cylinders got honed as they had no lip. new rings as well..
does this seem excessive?
gregor paid 1500 for a ford focus crate motor with no intake or exhaust. long block with head and belt. I will control costs better on the hi output motor next time.
trans was rebuilt with the heavy service kit for 800.00. ivan said it was all worn out inside--clutches, servpac and bearings. so I will see how she feels when I go back to my ref. the shifter cable issue will get a remedy with a one piece cable. fuel tanks are switched, so she looks a little more original from underneath.
the fish story I got was that the old man working my engine in machining has cancer and took a lot of time off. I will do this better next time. bitchen [craig] had a local rod shop that could have gotten this out with a new sized rod for maybe 800 to 1k.
I learn best when I stub my toes. engine hasn't come back from the machinist yet, even though it was promised today to me from last week--my engine guy went to vegas last weekend, so I think that's where his pricing is motivated from.
I haven't had this kind of work done for over 25 years, so it's almost like starting over.
fukushima/japan is getting worse--#4 reactor is melting down and they don't know how to stop it--
https://www.youtube.com/watch?v=ZkHKpGpMwTw |
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