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dsc00004.jpg (115827 bytes) Everett's 1965 Type 3 Ghia Log
Main page | Log

November 30, 2001 • Prepped car for possible sale tomorrow, took on test drive.
November 17, 2001 • Adjusted front brakes, bled brake system.
• Picked up socket extension, finished exhaust installation and all piping and hoses
• Started car, oil cooler seal is leaking, fan is making a horrible noise like it is rubbing on something.
• Left-hand carb. choke is sticking, spring for choke seems to have become dislodged.
November 16, 2001 • Installed exhaust, couldn't tighten top bolts because I need a longer socket extension (broke last one)
November 13, 2001 • Found one of the front left wheel cylinders was frozen, disassembled, cleaned and reinstalled:
Front brakes
• Assembled NOS exhaust for installation
• Attempted to bleed brakes (again!) but I ran out of fluid
November 12, 2001 • Installed NOS master cylinder, bled brakes, front left brakes are sticking, disassembled front left for examination.
• Installed new driver's door latch:
Old latch New latch
• Unfortunately the interior door pull broke:
brokenintlatch.jpg (52891 bytes)
• Vacuumed out door, it was full of dirt.  Cleaned and lubed window track. Misc door panel pics:
nodoorpanel.jpg (109436 bytes) driversdoorpanel.jpg (108683 bytes)
• Prepped exhaust and heater components for installation
• Ripped previous owner's cheesy vinyl off driver's upper door pad, there is one small tear, cleaned it up for reinstall until I buy a nicer arm rest.
November 11, 2001 • Went to a local VW show, found an NOS master cylinder, a replacement door latch, a nice used body-to-carb. air intake seal, and a few other misc. items.
• Cleaned and lubed driver's side door latch, cleaned air intake seal
November 10, 2001 • Checked out non-working fog lights - 1 bulb is missing, 1 is blown.  Fog light relay is also blown.
• Disassembled shifter to examine bushing, bushing is missing
• Removed stickers from windows and front and rear bumpers
• Cleaned front and rear plastic lenses
• Went and saw a 1969 Automatic Type 3 Ghia located in New River, AZ (north of Phoenix):
dsc00020.jpg (121071 bytes) dsc00028.jpg (104956 bytes) dsc00024.jpg (114853 bytes) dsc00012.jpg (98549 bytes)
Full details and photos here
November 7, 2001 • Cleaned up some wiring under the front hood relating to the fog lights, fog lights still don't work, I suspect a blown relay.
• Removed master cylinder to check it out.  Disassembled, the rubber seals are rotted and the body is pitted, time for a new one.  Broke out my NOS rebuild kit and NOS master cylinder but they are both for a Squareback (20mm bore instead of 19mm).
November 6, 2001 • Finished up some engine and ignition wiring.
• Cleaned up the routing of some fuel lines and primed fuel pump and carbs.
November 4, 2001 • Repaired starter solenoid wiring by cleaning up connections and running some new wire.
• Tested fix for oil light, it works, reinstalled fuel gauge cluster
• Finished install of new rubber brake hoses
• Exchanged broken tools and got the rear axle nut removed.
• Could not successfully drill out broken rear brake bleeder valve, replaced wheel cylinder
• Adjusted brake shoes, set e-brake handle
• Bled complete brake system twice but brakes are still weak, possibly need new master cylinder...
November 3, 2001 • Troubleshot starter system some more: Still have a poor connection from the regulator to the fuse box, made note that a "dealer fix" on another T34 was to run a new wire from the regulator to the fuse box.
• Installed new rubber brake hoses, tried to bleed rear brakes but one bleeder valve is missing
• Broke a few tools trying to remove the driver's rear axle nut
• Cleaned and greased front end
November 2, 2001 • Reset steering wheel, it was off a little.
• Troubleshot starter system some more: Found poor connections at regulator underneath back seat, cleaned up connections
• Ripped out wiring for aftermarket starter button
• Built wiring loom for tachometer
• Broke a few tools trying to loosen all the lug nuts
November 1, 2001 • Reassembled column and turn signal stalk, spent an hour or so getting turn signal column to self-cancel, greased all parts and adjusted steering wheel canceling ring
Troubleshot starter system:
• Removed starter, cleaned internals per Type 34 club web site
• Remove tranny to body ground strap, cleaned, and reinstalled
• Tested ignition, still won't start with key, voltage is still 4v at starter
• Tested with 6v helper solenoid, car starts now 
October 30, 2001 • Finished reassembly of ignition and column wiring, remounted column
• Checked choke functionality, left-hand choke not working, repaired it with my hammer. Set chokes.
October 29, 2001 • Reinstalled repaired ignition switch
October 28, 2001 • Installed rebuilt carbs. with new fuel hoses and gaskets
• Installed new breather hose
ghia_engine.jpg (103240 bytes)
• Set valves for the first time, the heads look brand new!
ghia_heads.jpg (81485 bytes)
• Tore apart and repaired the factory ignition switch, someone went a little crazy with the splicing at some point in the past...
ghia102801_5.jpg (104700 bytes)
• Corrected factory wiring from ignition switch to starter solenoid.  It won't crank over with key and the wires get real hot, uh-oh.
• Figured out there must be a break somewhere inside the wiring loom for the oil light, I'll run a new wire when I install my tachometer loom.
October 27, 2001 • Finished up the carb. rebuilds per my shop manual, had to grab a few parts off a spare set of carbs. to fix the choke internals and linkage.
• Replaced driver's side heater box (small hole near exit) with a nice piece I found for $5 at a swap meet.
rustyheaterbox.jpg (55971 bytes)
• Fixed heater linkage for heater boxes and rear seat controls
• Spent a few hours trying to clean the interior up, I think it got a tiny bit cleaner.
• Cleaned engine tin and balance pipe
• Test fit tachometer I recently purchased, not Type 3 Ghia but it's old VDO and it fits nicely in the clock hole
October 13, 2001 • Spent a few hours repairing, rebuilding, and correcting the linkage and chokes on the left carb..
• Found the fuse box cover under some stuff in my garage, cleaned it up for usage.
September 9, 2001 • Cleaned up an original German fuel pump and plastic cover that I bought in Albuquerque in August, it came out pretty nice. 
fuelpumpcover.jpg (63098 bytes)
September 8, 2001 • Cut up the original rotted out exhaust so I can remove the upper heat exchangers
September, 2001 • Busy with buying and selling a '62 Bus
August 9, 2001 • I was in Albuquerque, NM picking up a Bus so I took some time to go check out a T34 at Discount, here are the details:
nm_62_1.jpg (123057 bytes) nm_62_5.jpg (122110 bytes)
Full details and photos here
August 9, 2001 • Cleaned front seats and rear seat bottom with upholstery cleaner, Nice!
• Examined NOS exhaust that was included with the vehicle, it appears to be a later exhaust (70s Type 3) as the tailpipe outlet is 2" and my original one is smaller (1 5/8").  It's made by Leistritz, anyone want to trade?
• Messed with rear trunk lid, trying to figure out why it won't shut all the way so it is flush with the body.  The lid rests about 2-3 mm above the body.  My latest theory - The rear trunk lid where the lid catch bolts on is bent downward, possibly from someone forcing the lid open in the past.  Opinions welcome, here's a photo (the air flow cover has been removed):
decklidgap.jpg (67594 bytes)
August 8, 2001 • Removed left-hand carburetor for rebuild
• Removed fuel pump, fuel lines, and original 64-65 only shut-off valve.
• Removed seats and vacuumed the interior and floorboards for a couple hours, I think it needs a couple more hours of cleaning.
ghia102801_3.jpg (97503 bytes)
• Removed battery, cleaned and de-scaled battery tray area, noted a couple tiny pinholes of rust.
ghia102801_4.jpg (82006 bytes)
• Attempted to adjust rear trunk lid latch to make it sit flush, no luck.
August 7, 2001 • Removed original rotted exhaust
• Removed right-hand carburetor for rebuild
• Corrected accelerator cable to get full travel, removed extra spring on center linkage installed by previous owner
August 6, 2001 • Troubleshot oil light not working - no luck
• First pass on degreasing the engine and tranny, many more to come...
• Fixed passenger side fresh air drain hose, dumped a zillion gallons of water through the fresh air vents to clear out the dirt and dust
• Sprayed out rear intakes to clear out rear drain holes
• Adjusted, cleaned and greased rear trunk latch and key assembly
August 5, 2001 • Troubleshot low beams staying on all the time, fixed by unhooking power (terminal 30) to fog lamp relay
• Corrected installation of fuses - 8 amp vs. 16 amp - in fuse box per wiring diagram
August 4, 2001 • Purchased at 113,720 miles
• Set points and timing, adjusted idle and mixture, corrected carb. linkage, synched carbs.  Added tranny fluid, repaired 1 axle boot.  Drove home from Chaparral, NM to Phoenix, AZ.  (About 450 miles)
• The selling family had a few other Type 3s, Full details and photos here

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