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Swing Lever Shaft Kit, Center Pin, Center Link, Installation
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Tcash
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PostPosted: Sun Jun 15, 2014 12:42 am    Post subject: Swing Lever Shaft Kit, Center Pin, Center Link, Installation Reply with quote

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Cutting the 1/2"-13 threaded rod down to 12 inches.

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This is the layout to install the top bushing. Note I installed the thrust washer during installation, so the thick washer would bottom out on it and set the bushing installed height.

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This is the layout for the new parts.

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Showing installed order.

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This is the old swing lever set up.

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Using an 8" "C" clamp to put tension on swing lever while removing bolt. If you do not do this you will strip the bolt pulling it out.

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Remove grease fitting with 8mm socket.

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Tried using 20mm socket with extension and BFG (big freaking hammer) to drive bushings out. Switched to pressing tool and bushings came right out.

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Lubed threads with anti-seize.
Using pressing tool. 36mm socket on top, top nut I put on finger tight. This makes it easier to add sockets as needed.
Double nutted on bottom, with pressing nut in the middle. Hold the top double nut and turn the middle nut to press in the bushings .
Kept adding sockets on bottom until top bush pressed out. Removed top bush, put 36mm socket back on and continued pressing until bottom bush pushed out.

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Cleaned and lubed bore to except new bushings. Note bungee cords holding swing lever out of the way.

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Old parts. Note rust and wear on top of pin.

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Note shoulder on old bolt is longer. I would have liked to have used this again. But I stripped it pulling it out.

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I measured old bushings before I pulled them out and noted the wear pattern was from the front to back direction on the bushings. So I filed grease relieves into the sides of the new bushings. Important: when installing bushings they need to be oriented so relieves are side to side, facing the wheels. Not front to back.

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I used the old pin as a guide to start new bushing, with a few light taps of a hammer. Then I switched to pressing tool to send it home. Hole facing wheel.

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Pressed bottom bushing home. Note Grease relieves facing wheels.

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Pressing top bushing in. Top thrust washer installed to act as a stop to set bushing height.

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Note I marked the bushing to orient the hole toward the wheel. Thrust washer installed and pressed bushing home.

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Note top bushing sticks out to locate the thrust washer.

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This made installing the seals so much easier.

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Installing top seal. Thrust washer in the background.

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Fitting pin seal and packing washer on pin. The pin seal will hold the pin in place while you line up the swing lever and "C" clamp. Crappy picture. You can't see it, but there is a groove in the bottom of the Swing Lever. That the seal packing washer sits in.

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Lining up "C" clamp. Note the new pin protruded threw the swing lever slightly and required a washer to allow for this. The old pin wash flush.

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Applied anti-seize to lock plate.

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Using the "C" clamp to apply pressure to install the bolt. I might add I used an alignment tool to line up the hole. A big phillips screwdriver would work also.

Hope it helps
Tcash




Thanks to jerseylooker
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Center Pin Bushings I
Center Pin Bushings II
Replacing the Center Pin
Swing Lever Shaft Kit Installation
Swing Lever Tool... homebrew?
How to replace centre pin for steering.
How to make your bus swing lever bushings real tight, no play


Last edited by Tcash on Fri Dec 25, 2015 8:17 am; edited 4 times in total
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Joey
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PostPosted: Sun Jun 15, 2014 5:50 am    Post subject: Reply with quote

Nice!

I suggest to keep the wavy washer from the old set up as I find the new ones have a tendency to break shortly after installation...
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webwalker Premium Member
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PostPosted: Sun Jun 15, 2014 10:07 am    Post subject: Reply with quote

Thanks for your fantastic contribution to keeping our rides on the road!

I'd love to see someone who is installing a new front beam perform all of this work while the beam is out so that you're not fighting to get a good shot while standing on your head underneath the car. (I've been there with ya on this; you need four arms.)

Maybe I'm the someone, but I don't need to take my front beam out...I don't think...yet.

Anyway, great job!

M
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highlandmurf
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PostPosted: Mon Sep 01, 2014 6:35 pm    Post subject: Reply with quote

Just replaced my center pin today.

A big thanks to this thread and others.

Just a couple of thoughts while it's fresh.

I had to press the bushings out through the bottom. I found that the shift rod did not give me enough clearance to use the 36mm socket up top.

I stripped the original bolt putting it back in. I would have preferred to use it, as it was a little different than the new one (smaller head, and a slightly longer shoulder)

I had to take the new one and thread it through backwards to clean out the metal filings.

The clamp may have misaligned the two parts of the swing arm causing the bolt to cock to the side.

I found rocking the swing arm while I fed the bolt in allowed me to get it in hand tight all the way until the nut came in contact with the swing arm.
When it goes in it goes in easy. If not, figure out what is wrong.



Gotta love when your new parts say West Germany!!!

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Thanks again for the great write up.
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knightsofni
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PostPosted: Fri Sep 26, 2014 5:03 am    Post subject: Reply with quote

Excellent write up!
I found your pictures extremely useful.
Not to take anything away from your post, but some things I found were;

Your pressing tool looked great but I had no threaded rod so I removed the old bushings with a hammer and an old impact socket.

I thought that the top packing washer and pin seal were missing, however the PO put them on in reverse order and they were stuck up in the relay lever!
That would not have sealed at all! No wonder it was a greasy mess

To reinstall the new bushings I ground down the pin as others suggested, worked great.

I also had to heat the bigger top seal to get it on, I must have fought with it for 1/2 hr. In the end I put it on the grill of my work light for 30 seconds and it popped right on. RELIEF!

The hardest part for me was re-aligning the groove in the pin with the relay lever, I found the clamp got in the way.
Instead of the clamp I used a bottle jack under the pin to compress the spring. This allowed the relay lever to move freely for alignment.

Thanks again for your walkthrough it gave me the confidence to even start the job, and my steering is vastly improved Very Happy
Knights
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PostPosted: Fri Sep 26, 2014 7:29 am    Post subject: Reply with quote

knightsofni wrote:
Excellent write up!
I found your pictures extremely useful.
Not to take anything away from your post, but some things I found were;

Your pressing tool looked great but I had no threaded rod so I removed the old bushings with a hammer and an old impact socket.

I thought that the top packing washer and pin seal were missing, however the PO put them on in reverse order and they were stuck up in the relay lever!
That would not have sealed at all! No wonder it was a greasy mess

To reinstall the new bushings I ground down the pin as others suggested, worked great.

I also had to heat the bigger top seal to get it on, I must have fought with it for 1/2 hr. In the end I put it on the grill of my work light for 30 seconds and it popped right on. RELIEF!

The hardest part for me was re-aligning the groove in the pin with the relay lever, I found the clamp got in the way.
Instead of the clamp I used a bottle jack under the pin to compress the spring. This allowed the relay lever to move freely for alignment.

Thanks again for your walkthrough it gave me the confidence to even start the job, and my steering is vastly improved Very Happy
Knights


you need a c-clamp to pull the arm towards the head of the pin before you tighten the bolt. You need to get all the play out of the assembly that you can.
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guanella74
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PostPosted: Sun Nov 02, 2014 7:25 pm    Post subject: Reply with quote

I'm looking for just the seals to redo the center pin, not the full $50-75 kit.

Might anyone know where I can find the pin seal and the outer seal?
Huge thanks,

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Professor Dred
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PostPosted: Sat Dec 06, 2014 10:56 am    Post subject: Reply with quote

I'm trying to do this right now. I've got the pin out but I can't for the life of me get the bushings to budge. I've tried this setup and hammering on a socket but nothing is working. Any other suggestions? Bently says use a slide hammer but I have no idea what size it needs or where I should try to find one.
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busdaddy
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PostPosted: Sat Dec 06, 2014 11:15 am    Post subject: Reply with quote

A regular hammer and socket pounding up is just as good as the slide hammer pulling it down, no need for that.
If the socket you are using has a rounded edge where it's against the edge of the bushing it may be trying to expand it opposed to pushing it cleanly, find something with a sharper lip or grind the socket flatter. The grease fitting is removed, right?
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Wildthings
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PostPosted: Sat Dec 06, 2014 11:22 am    Post subject: Reply with quote

Professor Dred wrote:
I'm trying to do this right now. I've got the pin out but I can't for the life of me get the bushings to budge. I've tried this setup and hammering on a socket but nothing is working. Any other suggestions? Bently says use a slide hammer but I have no idea what size it needs or where I should try to find one.



I made this tool from an old shaft. I can apply a lot of force with it using a Grade 8 bolt.

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I also had a tool designed for beating the bushing out made up by a local shop. It too will apply a lot of force. What weight hammer are you using? A 3# hand drilling hammer or a 3-4# sledge should do the job easily.


.
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Professor Dred
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PostPosted: Sat Dec 06, 2014 11:30 am    Post subject: Reply with quote

Yes, the grease fitting is removed. I'm using a standard hammer and a spark plug socket. I will try to grind it but I've tried the back side that's pretty flat. Don't have a bigger hammer right now. I would think it would move even slightly. I do have an air impact hammer though.
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Tcash
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PostPosted: Sat Dec 06, 2014 1:18 pm    Post subject: Reply with quote

Professor Dred wrote:
Yes, the grease fitting is removed. I'm using a standard hammer and a spark plug socket. I will try to grind it but I've tried the back side that's pretty flat. Don't have a bigger hammer right now. I would think it would move even slightly. I do have an air impact hammer though.

To my surprise. I had no luck trying to pound them out. The pressing tool worked easily though.
The air hammer is worth a try.
Good Luck
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PostPosted: Sat Dec 06, 2014 1:28 pm    Post subject: Reply with quote

Finally got them. What a bugger. Hammer hammer hammer hammer. Those were in there tight. New ones are in. Working on the plastic seals now. Thanks.
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PostPosted: Sat Dec 06, 2014 7:33 pm    Post subject: Reply with quote

Professor Dred wrote:
Finally got them. What a bugger. Hammer hammer hammer hammer. Those were in there tight. New ones are in. Working on the plastic seals now. Thanks.


Just did mine with a copy of the tool on page 1. Using the all thread puller, they came out smoothly, and same tool pressed in new bushings.

I was dreading this job, but thanks to Tcash, the job was easy, I did it in 2.5 hours. This was so easy, I would NEVER dream of using a hammer. Now I wonder what I was worried about.

Many, many, Thanks to Tcash. awesome tool. this procedure ought to be a sticky!
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PostPosted: Sat Dec 06, 2014 7:35 pm    Post subject: Reply with quote

Professor Dred wrote:
Finally got them. What a bugger. Hammer hammer hammer hammer. Those were in there tight. New ones are in. Working on the plastic seals now. Thanks.


Here is the good news for all that fight with it. Once you pull that center pin and bushings out and replace them, you are officially a VW mechanic. Smile It is one of those jobs that one has or has not done, and you can now say, "Yeah, I did mine." Kudos and job well done Smile
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Professor Dred
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PostPosted: Sun Dec 07, 2014 3:42 am    Post subject: Reply with quote

larryducas wrote:
Just did mine with a copy of the tool on page 1. Using the all thread puller, they came out smoothly, and same tool pressed in new bushings.


I also want to thank Tcash for his write-up. I tried to use the tool to remove them. Didn't work for me. I ended up bending the smaller washer with it. My entire replacement took almost all day. The socket and hammer were the only thing that got mine out. I'm sure all of the cussing helped too. (Just glad my mother was not anywhere near.)

Now, the tool worked great getting the new ones in. I could not see the source of the 'play' I was seeing while the old ones were in, but the two things I didn't see when pulling it all apart were the plastic seals. Doubt those were the culprit though.

Two thing's I want to note for my '71. I couldn't get the large socket and a nut to fit on top due to the shifter bar so I had to work backwards with the socket on the bottom. And my grease fitting took a 7mm, not 8.

And SGKent, I've done so much to this bus that I never would have dreamed of before I already considered myself above the bar. But yes, this will go down as one of the most intimidating jobs to start, and one of the most frustrating jobs after starting, then one of the most worrisome jobs while struggling with it. Really thought I was screwed here.
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PostPosted: Sun Dec 07, 2014 3:46 am    Post subject: Reply with quote

I must also note, I've replaced everything dealing with the steering now except the gearbox and boy does it feel great. I have just an inch or two of back/forth play in the wheel and I've adjusted the gearbox to get rid of the click while still having tight handling. The true test on the road will have to be a while. I started trying to replace my torsion leaves yesterday but now I've decided to buy a new bundle instead of putting the originals back in. Also going to do my ball joints and wheel bearings while I'm there. There is 40 year old grease all over the place and the ball joints look horrid. After that, the whole front end will be new.
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PostPosted: Sun Mar 08, 2015 6:04 pm    Post subject: Reply with quote

Thanks for all the tips... And just a reminder, for those of us who can be dim at times, the bolt that goes into the swing lever arm doesn't have a nut on the end, the arm has threads in it. It's been a few months between disassembly and assembly again, and I though I couldn't find the right nut and bolt. Wondering why the bolt won't go through, the tiny dollar store mirror I have to look into the hole showed threads! Wink
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PostPosted: Wed May 27, 2015 1:20 pm    Post subject: Center pin Reply with quote

Changed mine out Sunday your post was very good and helped me a lot. Thanks TCash
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PostPosted: Sat Jul 04, 2015 4:20 pm    Post subject: Reply with quote

I used this method last weekend to change my center pin. Thanks Tcash for a great write up.
Image may have been reduced in size. Click image to view fullscreen.

The C-clamp fits under the shift lever in just the right spot. I had a clamp with a missing swivel and the ball end fit nicely in the divot at the bottom of the pin
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I used extra leverage to reef the clamp tight
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Threaded rod tool pushed the bushings in & out with ease
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